著者
古家 和彦 磯江 浩 帆足 博明 平野 茂
出版者
社団法人 日本鋼構造協会
雑誌
鋼構造論文集 (ISSN:18809928)
巻号頁・発行日
vol.10, no.39, pp.131-141, 2003-09-30 (Released:2010-06-28)
参考文献数
8

Due to the Geiyo Earthquake in March 24th, 2001, center stay rods of the 1st Kurushimakaikyo Bridge(suspension bridge) were broken. They were designed to break in strong earthquake and work as safety valve of the structure. In order to evaluate the mechanism of the breakage of the rods, data from field measurement were processed using structural analysis, and it was confirmed that the broken rods worked as designed. It also was confirmed that forces acted to other unbroken rods in 2nd and 3rd Kurushimakaikyo Bridges were not large enough to affect their soundness. Through this experience, it was proven that field measurements and structural analysis can be effective tools not only for design but also for maintenance of structures.